Airborne Avid

 

Short finals for NZFI  10

 

At last, after 10 months and nearly 700 hrs of work, JHW was ready to go – well almost.  I had to add the water, oil and fuel, and make sure they and the electrons went in the right places at the right time. I was about to learn yet another lesson…

 

I’d arranged hangarage at Fielding and been made most welcome by the Manawatu Microlight Club, which I’d joined some weeks before. It’s a great bunch of people, with a positive outlook, good facilities and well worth the two hour drive from Wellington. That drive has now become a regular event. I became used to it quickly because once JHW was ready to run, the skies decided not to play ball, and it was 7 trips and weeks later before I could fly. JHW was delivered to the hangar on the 3rd of August 2003, but not flown until the 18 October. All week the sky would be lovely, then crud for the weekend, nice again on Monday. Again and again. I learned patience. I learned the back roads to Fielding. I learned how tolerant Judith is.

Finally, a Saturday arrived when I could at least run up the engine and check out the various systems. Roger Dixon and John Varley again helped, abused and cajoled. All the fluids were in, we were ready to go.

 

STRIKE ONE

The first job was to make sure oil was getting to the engine, as the long break and disconnected lines meant that the galleries and pump were empty. Now the fun really started. We decided to pull the engine through by hand to prime the pump. After 20 min, much sweat and tired arms, nothing had happened. We loosened the connections at the engine (uphill end), and used 5 psi to blow oil from the tank to the engine, then tightened it all up and cranked again. Still nothing. This time I removed the feed line to the pump , set up a funnel and poured/cranked in 500mls. Reconnect the line, hand crank and  - bingo – twitches on the pressure gauge. Right – time to do it properly. Fuel taps on, electric pump on for 15 sec, then off as it loaded up, full choke , a few turns and at last JHW was alive again – then horror , the oil pressure dropped down below 20 psi – switch off.

New diagram                          Old diagram

Note lower sketch

 
We tried again – same result. After an afternoon of frustration and zero progress, I went home to have a break and a rethink. We’d followed the manual with the installation, pre-filled the lines and pump, and still both lines would be empty after a 10 second run. The solution came from an unexpected direction. I’d been working from the July1998 manual that came with the plane. In section 9.3 on the lubrication system, there is a nice front view drawing of the engine, oil cooler and oil tank. The tank detail shows that the angled tube is the feed, and goes to the bottom of the tank, while the vertical tube is the return. BUT when I looked through the ROTAX CD, at home on the computer, I found a nice isometric sketch that showed the top of the tank with the tubes reversed. The angled one was the return, and the vertical one the feed. The difference is that the front projection diagram in the 98 manual showed the VERTICAL COMPONENT of the angled tube, and the ANGLED COMPONENT of the vertical tube. Had the diagram been drawn from 90 deg around the correct relationship would have been obvious. The new CD has a nice perspective sketch which clears this up instantly. I can only assume I’m not the only one that had been caught!! I’d also used a generous amount of oil, so there had been enough to just start to fill the wrong line from the tank, get a pressure indication, and then start the engine and blow it back the wrong way.

John Varley and me on the way to Waipukurau

 

 

The next weekend we were up there full of enthusiasm, 10 min to reverse the connections and JHW was fired up, oil pressure excellent, and I proudly taxied around to the MMC club rooms.

 

STRIKE TWO

After a number of club members had had a good nosey around, and Bill Penman had reassured me for the tenth time that I was quite capable for the test flight, I started up and this time got as far as mag checks. On each side , a massive 1000 rpm drop, and exactly the same feeling rough running. Back on both,it ran sweetly. R or L alone and 1000 down, lotsa shakes. What the hell was going on? Off with the cowl, pull plugs – all nice. Make sure the plug leads were firmly on, check the connections on the back of the switch – all correct and secure. Run up – same result. I had run out of ideas, so I asked John Bolton-Riley to have a look around, while I took a student in the Xair. I figured that a change of pace might help and a new brain looking at the wiring might be useful. Trouble was, I picked the brain with the most sadistic lack of tact in the club. JBR was waiting with a big grin after I emerged from the Xair some 40 min later. The conversation went something like this…

JBR – “Havill – you’re a school teacher, right? “

PJH  - (with some trepidation) “Yes”

-         “Do you know how to count??” (sadistic grin, and knowing leers from those within earshot)

-         er – yes”  (Why the hell did I ask him? )

-         “ go and look at the numbers on the HT leads” (evil laughter)

I did . I’m dumb – REALLY dumb. The top leads on #2 and #4 were reversed. ARRRGGGHHHHHH! <insert your favourite language here>. I reversed them. The engine ran sweetly. Mag drops were minimal. The club was entertained greatly, and strike three began polishing its’ opportunity, shortly to be employed.

At last the time had come, and I was about to test fly my beautiful rebuilt Avid. I’d dreamed of this day for months, and here we were, all problems fixed, a lovely day, supported by club mates capable of the highest and most thoughtful levels of personal abuse. It doesn’t get much better.

 

“Post JBR”  mag check        (Photo Bill Penman)

 

STRIKE THREE

I fired up, checked everything about three times and taxied for 28 grass. The radio worked well, noise canceling headset was great, etc – all sweet. I called “Fielding traffic, Juliet Hotel Whiskey lining up 28 grass for test flight”, turned onto the grass, took a deep breath and open the throttle. It worked! We had a reasonably straight, slightly protracted take-off. All the numbers looked good, and the Avid flew well as I tracked around the circuit and called the traffic to advise I was climbing to 1300’ overhead the field for 20 min. My plan was to orbit overhead, look for stable temps, feel out the plane and generally get my feet used to the rudder pedals again. This was going to need some practice, as the ball slammed from one end to the other. I decided to stop trying and lo and behold, it stopped ricocheting around the panel. After about 12 min, the third strike surfaced. I heard a PHUTTT sound from behind the panel, and white smoke poured out and rapidly filled the cockpit, IFR with the cloud enclosed in the cabin! It stunk horribly of burnt paxolin. The first priority was fly the plane. Everything was still working so there were no worries there. A brief crack of the door cleared most of the smoke, and I called “Fielding traffic, Juliet Hotel Whiskey has smoke in the cockpit. Joining downwind and expediting landing”. Bill Penman immediately replied to check that I was OK, and then left me to get on with the somewhat abbreviated circuit and landing. I hadn’t called PAN PAN PAN because I was already at the right place, and the fault had not caused any difficulties in the handling of the plane, nor had it affected the running of the engine. As I descended to my brief circuit, I thought about what was behind the panel and decided it was almost certainly the large 22000 microfarad capacitor that smoothes the voltage regulator output. For some reason it had spat the dummy. I decided that fire was unlikely as the smoke had come with sound effects, then no more - yes it had to be the cap.

Landing was uneventful, and on return to the club room, and removing the upper cowl, we found that the cap had indeed blown, spraying evil smelling yellow muck all over my nice neat wiring. My voltage regulators had protected apparently protected the radio, comms and GPS from any spikes, so all there was to do was to cleanup, remove the cap and organize another.

 

I tracked down a replacement from Auckland, ($109) and also learned what probably happened. After the big smoke

 

First of all, several people told me that electrolytic caps, if left for a long time with no voltage applied, can suffer degradation of the dielectric layer. When powered up again, they can “cook off” as mine did. The other contributing factor was that the maximum working voltage of the capacitor was 25 V, and the regulator can put out 33 volts (no load), so really at least a 35V, or preferably 65V rated capacitor would be indicated. The remaining unknown was that in the process of cleaning up the mess, I’d disconnected the “alternator disconnect” relay and so later, when re-installing, was unable to be sure that my problem had not been caused by a mistake in connecting the relay to join the output of the rectifier to the battery (load). This system is needed to prevent the battery from discharging through the rectifier and alternator when the engine is off ( aircraft is left in the hangar for a week or two –flat battery).

Whatever it was, the replacement works OK and all seems well now.

 

 

LESSONS (RE)LEARNED

 

Always, always, always arrange for another brain to cross check your work. Especially, arrange for them to take the time for a thorough, leisurely and undisturbed check of electrical, fuel and oil systems. Where I got caught was that many friends had looked over my work as it had progressed, helped, fixed problems and been involved in very knowledgeable ways. Each part of each system was checked, but only one brain looked at the whole thing, and that had been too close for too long. The Annual condition inspection given prior to flight was thorough and picked up a few split pins, washers etc as such inspections go, but not any of the more tricky permutations that surfaced as we tried to get JHW airborne.  Nor was it the function of such an inspection. What I was pleased about was that when something went wrong in the air, I FLEW THE DAMN PLANE FIRST, and troubleshot second. I’d spent some time thinking about the test flight, planning what to do for engine failures at various stages, total electrical failures etc. As usual, the inflight problem you often encounter is not exactly what had been planned for, but the decisions made weeks previously worked like clockwork. Overall it had been a most satisfactory process.

 

 FLY TIME J

 

Once the new capacitor was fitted, JHW was away. The following weekend was a real pleasure – I took my son Robert as my first passenger, then Roger Dixon (general workshop pariah and abuse merchant). We did a couple of hours and went home well satisfied. Rog and I had been complete idiots once clear of the circuit, cheering , yelling and yahooing in the cockpit like the real pillocks we profess to be.

 

The next weekend was a real eye opener. We went up to Fielding to play in the plane. By the end of the day, I’d done 6.2 hours – more flying than on any other day in my entire experience. I took anyone for a fly, my daughter Annelise, JJ , a trial flight, John Varley, and a couple of other club members. I was amazed at the contrast to MYC, our Challenger. In the Avid, a 20 min flight took us to Woodville and back. John and I headed for Dannevirke, decided it was too quick, and went on to Waipukurau and back. These would be quite reasonable cross-countries in MYC, but were a doddle in JHW. What a blast.

Jennifer still smiling as we head back into the sunset

 

 

I also had a chance to take Peter Dunning and his daughter Jennifer for a fly. Peter and I have become close friends as committee at club level, and building our machines. It was a great early evening fly, and for Jennifer, a literal eye-opener. She’d had a Bantam ride in less than ideal conditions a couple of years previously, and was a little unsure of another microlight flight. As we lifted of the wide-eyed “Wow” from the right seat was music to my ears.

 

We’ve been at it since then – any excuse for a fly and since that 19 October test flight, JHW has logged 44 hours, including a 24 hr/ 10 day excursion down the east coast of the South Island, stopping at Waimate to stay with the inlaws and visiting Croydon Aircraft at Manderville (excellent – GO THERE  - trust me – just do it)

And managed to catch up with Stuart Tantrum  at Omaka and have a look at the WW1 collection there. I learned a lot about transponders, controlled airspace, the Canterbury nor’wester and made a couple of good weather decisions. Maybe that will be another story, although  I might leave it for a few issues as you all have had to work through 4 Avid articles in a row.

Peter Hancox – he helped me with the original purchase of JHW (see episode 1)

 

 

Summary

The bottom line is that the whole process has been very satisfying and I have a plane I’m passionate about (as if you couldn’t tell ), I’m intimately familiar with all it structure and systems, and have much to learn in the flying, and ground handling side of things – all of which I set out to do. Yes it was a good decision to buy a tired plane and rebuild it, and yes there are still some compromises I must live with, particularly a limited baggage space (compared to a RANS).  It flies well although I only get about 5200 rpm at takeoff, instead of the preferred 5800, but in the air, 5500 yeilds 100mph and 5200 about 90. I have much to learn about wheeler landings and can manage 3 point OK. I can fly for 30 min, just touching the rudder pedals occasionally, perform really good slips, and bank angles way beyond the capability of our Challenger. 44 hrs in 3 months is great and by the time I reach 100 hours I’ll be well on the way to learning the niceties JHW is capable of. In the meantime, JBR has come up with a cunning plan involving the Chatham Islands. Any other Avid drivers out there interested?

Heading down the Kaikoura coast, Jan 04